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Figure 1: Close-up shot of the repair. |
Wednesday, June 3, 2015
WEEK 10.1: FIXING A CRITICAL ISSUE
Today while we were testing the machine for reliability, we ran into the issue were the valve became detached from the reservoir tank. Acting quickly, we simply cleaned off the dried up rubber cement, reapplied a fresh coat of primer and rubber cement and waited for results which can be seen in Figure 1. Currently, the valve is holding up with no immediate issues faced. Hopefully, this will be able to hold up for the final presentation.
WEEK 9.LAB: PRACTICE PRESENTATION
Today's lab was a simple task as we were asked to give a test presentation of the one we give next week as the final. With our powerpoint presentation about 70% complete, we presented to the best of our ability. Below (Figure 1)is a screenshot of the title slide in the presentation. Making note of what we need to change, add, and improve, we will be sure to be prepared for the final showcase.
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Figure 1: The title slide of the powerpoint presentation |
WEEK 9.2: ASSEMBLING THE MACHINE (PART 2)
With the deadline steadily approaching, we decided that today would be the day that we finish the machine. With the tubing attached to the valve, all there was left to do was to incorporate the microprocessor and tinker with the design a bit. We decided to add construction paper and leaves to the exterior in order to mask the sheer dullness of a drawer set. Figure 2 shows the machine nearly complete with a few minor details remaining.
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Figure 2: Full shot of entire machine |
WEEK 9.1: ASSEMBLING THE MACHINE
The focus on the meet-up for today was to make sure that the tubing we have would be able to fit in the valves. An issue we ran into was that tube was indeed a bit too small. As a response, we simply applied scotch tape over the end of the tube until it would fit in well. Once the sizings were just right, we applied a primer to the tubing which would maximize the effectiveness of rubber cement (as seen in Figure 1). Unfortunately, this took multiple attempts as we would run into the issue where the tape would slide off of the tube or the rubber cement would would allow a few leaks here and there.
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Figure 1: Close-up shot of the tubing bonded to the valve |
WEEK 8.LAB: SUCCESS WITH THE SECOND DRAWER
We came into lab this week expecting to struggle through cutting our second drawer with nothing but a box cutter. However, things turned out better than expected
At first, we tried cutting through our drawer with a box cutter again. We realized quickly that this was causing our drawer to crack and split, most likely because of the temperature of the room being too cold. To overcome this, we decided to take our drawer into the machinery room and have a TA saw through it with an automatic saw. This method proved effective. Though we had to make the slot in our second drawer slightly larger than the first due to initially cracking parts of the drawer with the box cutter, (as seen in Figure 1), we were happy with the outcome of the lab. After all, our second drawer doesn't need to be as strong as our first drawer, which will be bearing the weight of the reservoir tank.
At first, we tried cutting through our drawer with a box cutter again. We realized quickly that this was causing our drawer to crack and split, most likely because of the temperature of the room being too cold. To overcome this, we decided to take our drawer into the machinery room and have a TA saw through it with an automatic saw. This method proved effective. Though we had to make the slot in our second drawer slightly larger than the first due to initially cracking parts of the drawer with the box cutter, (as seen in Figure 1), we were happy with the outcome of the lab. After all, our second drawer doesn't need to be as strong as our first drawer, which will be bearing the weight of the reservoir tank.
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Figure 1: Full shot of the two drawers |
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